WILLIAM KIM ANGEL
*** *** ****** *****, *******, NC 27006 • Phone 336-***-**** • ******@******.***
INDUSTRIAL / MFG. / LEAN ENGINEER / MANAGER / SIX SIGMA BLACK BELT
BACKGROUND SUMMARY
Consistent track record of improving manufacturing and warehousing metrics utilizing a unique combination of excellent education, industrial engineering, lean, six sigma, and practical hands-on experience. Use engineering, manufacturing and team skills to cut costs, improve quality and forge strong internal customer relations.
PROFESSIONAL EXPERIENCE
O’Neal Steel, Inc. Greensboro NC, www.onealsteel.com [Formed Steel Service Centers]
Atlantic Region Operations Manager June 2009 to Oct. 2010
Responsible for continuous improvement of operations and creating an atmosphere of change in six plant facilities including the following areas.
• Lean Deployment Strategy: – led Lean Steering Committee meetings, trained and coached.
Revitalized Lean Program throughout the Region (6 Districts in VA, NC, FL)
Initiated 42% increased Lean event activity
Led 5S Program in two Greensboro Districts
Instructed team leaders on A3 report documentation and project planning
Wrote (59) equipment checklists for operators with maintenance and 5S criteria
Developed 5S audit criteria, trained auditors (supervisors), monitored their performance on plan
Compiled electronic Factory Visual Board content, regularly updated metrics on safety, 5S, efficiency, quality, and on-time delivery
Utilized Lean Assessment scores to launch lean activity in weak areas
• On Time Delivery: - Introduced Six Sigma DMAIC methodology to reduce on-time delivery errors.
Led first Team Project to success in 49 days, on time reducing errors by 60%, projected revenue savings of $330K annually
• Productivity: - Introduced production efficiency metric and reporting.
Trained Production Managers in managing efficiency
Pioneered systematic down-time reporting and analysis of data
Trained techs in time-study and cycle time checks
Performed shop floor training of supervisors to troubleshoot efficiency roadblocks
Measured work content by time-study
Analyzed the accuracy of current router rates by graphical means
• Safety: - Promoted MVP (Managing Vital Performance) behavioral-based safety system.
Trained Management and supervisors
Monitored auditor performance
Conceptualized MVP Improvement Team, led two teams, took action on low score areas before recordable incident occurred
• Reporting to Executive Leadership:
Analyzed and reported Regional performance on the following metrics:
Safety (OSHA Rate) - On-Time Delivery
Expense as a % of Adjusted Gross Margin - Quality Delivery Rate
Lean Deployment Strategy event activity
• Coordinated Corporate mandated improvement programs throughout Region related to cost savings, safety, Lean, regulatory compliance, HR Policy, etc.
K.B. Properties L.L.C., Clemmons NC [Real Estate/Finance]
Member / Manager Apr 2001 to June 2009
Resigned Hayward to enter an entrepreneurial enterprise.
Co-founded residential real estate investment holdings company. Buys, sells, and leases residential properties.
Hayward Industries, Clemmons NC, www.haywardnet.com [Plastics/Assembly]
Mfg. Engineer / Industrial Engineer Jan 1997 to Apr 2001
Recruited from AMP for substantial raise, expansion of skill set into manufacturing engineering, process, and packaging. Responsible for all engineering activities, except design, for four (4) production assembly lines.
• Quality Functions – $458MM Company required no separate Quality Assurance Engineer:
Implemented test procedure and random sampling of under water pool light electrical connections
Troubleshoot injection molding, urethane molding, secondary machining and assembly QA issues
Specify and/or modify plastic injection molding and secondary machining critical dimensions
Re-design urethane and injection molded components for manufacturability including tooling modifications
Designed automated under water pool light water test unit, developed test procedure, trained inspectors
Re-calibrated and certified chlorinator air pressure leak tester after maintenance rebuild, involved sampling
• Cartridge Filter Assembly Line – first year accomplishments on this line:
Relocate line to marry to in-house customer line, eliminates material handling
Timestudy/Line Balance for a 49% labor productivity increase
Line-Height Adjustment & Ergonomic Improvements using Add-a-Level platforms and scissors lift
Add tooling to facilitate speed, jib-pole boom, tool balancer, torque arm, air driver, custom head
Ergonomic improvement, UniMove Vacuum Lift to eliminate back strain when palletizing
• Chlorinator Line – example cost savings project – Line Integration with Re-Design and Sonic Welding
of Plug:
Re-designed previously glued component to facilitate ultra-sonic welding, changing joint design
Pioneered ultra-sonic process, justified and wrote CAR, developed process parameters
Developed and performed weld joint testing up to 200 psi to assure leak integrity
Re-engineered assembly process to integrate machining processes, marrying two production lines
$11,565 savings in WIP inventory carrying costs – cut in half
$3,837 floor space savings, (5) backflush inventory lanes saved
$2,222 indirect labor savings in material handling, increased line output from 705 to 842 pcs per shift
$5,203 savings in elimination of 79 planning work orders per year
Achieved management objective of adhesive elimination and 24 hour cure time, facilitates one-piece flow
• Underwater Pool Lights and Spa Lights – avoided capital investment in line duplication:
Spa Lights – engineered a 65% direct labor productivity increase on a line with 9 assemblers
Pool Lights – engineered a 14% increase on a line considered “maxed out” in regards to output
• Urethane Molded Element Line – project to relocate and improve the top scrap producing line in the
Company:
Relocated line from Pomona, CA to Winston-Salem, NC transparently to customer
Developed chemical ratio measurement procedure, trained operators
Wrote 19 maintenance work orders to improve line production equipment for quality capability and process control
Designed molding fixture modification “poka-yoke” called a pleat comb to address the #1 defect
Decreased machine processing time on bottleneck operation pleater
Specified tooling modification to urethane molds, corrected two rejectable dimensional problems
Implemented nitrogen blanketing process to aid preservation of raw material chemical in drums
Modified the composition of urethane chemical to decrease moisture sensitivity at no cost
Resultant process yielded a scrap rate well within Hayward quality standards and higher output
Capital appropriations projects, justification, & implementation; production methods improvements and cost savings through new equipment, fixturing, & line balancing; process engineering of urethane molding, ultrasonic welding and secondary machining; standard rate development; layout; troubleshooting; implementing design change; new product support; packaging development.
• 1997 Cost Savings $75,419, logged six cost savings projects
• 1998 Cost savings $101,437, logged thirteen cost savings projects
• 1999 Engineering support for nineteen (19) new products
• 2000 Formal training and experience in kaizen methodology and lean manufacturing, JIT, cell design,
5S, Poka Yoke through TBM Consulting Group, www.tbmcg.com. Served as team leader, trainer, team member, and engineering support for breakthrough events.
AMP Incorporated, Winston-Salem NC, www.tycoelectronics.com [Electrical Connector Mfg.]
Operations Engineer June 1995 to Jan 1997
Recruited from Burns Aerospace for raise and an opportunity with a world-class manufacturer in a boom market.
Capital equipment justification, approximately $2MM in 1996; maintain standard cost for Data/Infoport Team - rates, routings, wkctrs, BOM’s, ovhd; plant layout (MEDUSA) - plan related facilities and maintenance work; capital budgets; operations engineering analysis such as in/out sourcing, cost/savings, & capacity, ISO 9001 compliance.
• Awarded two spot bonuses for outstanding performance • Promoted to Engineer Level II
• Awarded Certificate of Commendation for significant contribution to the Quality Improvement Process
Burns Aerospace Corp., Winston-Salem NC, www.beaerospace.com [Aircraft Seating Mfg.]
Industrial Engineer Aug 1993 to Jun 1995
Recruited from Ilco Unican Corp. Responsible for IE in primary and secondary machining operation.
Capital appropriations projects; cost reduction/mfg. improvements; cellular mfg. development; continuous improvement teams; costing; make/buy analysis; standards maintenance; plant layout (CADAM); job evaluations; mfg. supervision (temp).
• Pioneered secondary machining being performed within the primary machining cycle, still used today.
Ilco Unican Corp., Winston-Salem NC, www.kaba-ilco.com [Mechanical Lock Mfg.]
Industrial Engineer Mar 1991 to Jul 1993
Labor standards; product routings; bills of material; product costing using IBM MAPICS; incentive systems; methods improvements; job descriptions; utilization and efficiency reporting;
• Routinely engineered productivity increases on individual work centers of 35% to 150%
J.L. De Ball-Girmes of America, Inc., Asheville NC [Textile Mfg.]
Industrial Engineer Jan 1990 to Nov 1990
Responsible for all I.E. activities. Left due to plant shut-down.
• Increased labor productivity by 90% on one warping machine
EDUCATION
University of North Carolina at Asheville Central Piedmont Community College
BS in Industrial and Engineering Management, 1989 AutoCAD LT Windows 95, 1997
Graduated with departmental honors. GPA: 3.57
CSSBB Lean Six Sigma Black Belt Certification
American Society for Quality, May 2009
PROFESSIONAL SOCIETY
American Society for Quality
Central North Carolina Section - 1109